Expert HVAC Service in Niederwald TX
Since 1988, residents of Niederwald, TX have trusted Garner Heating & Air Conditioning to provide professional work and outstanding service for all of their HVAC needs. If you're looking for a provider you can count on, call today!
Yes, air conditioning units should be serviced in Niederwald, TX. Getting your air conditioning unit on a maintenance plan is a good way to ensure that your air conditioning system is cleaned, inspected and serviced on a regular basis. A well maintained unit typically lasts its full life expectancy and has fewer repair needs, whereas a poorly maintained unit requires many repairs, breaks down more frequently and has a shorter lifespan. To get your air conditioning unit serviced, contact us today.
Your home air conditioner may not be turning on in Niederwald, TX because:
- Your evaporator coil is frozen or broken.
- The circuit to your air conditioner has tripped.
- Your thermostat’s batteries are dead.
These are the most common reasons your air conditioner may not be working, but there are multiple reasons your air conditioner may not be turning on. If you are experiencing the last two issues, you may be able to fix it yourself. However, if your air conditioner is not turning on due to a different issue, you should get it repaired by an HVAC technician. Call us today to have your air conditioner repaired.
Your home air conditioner should be maintained at least once a year in Niederwald, TX. The best time to get your air conditioner maintenanced is in the Spring, right before summer when you will be needing your air conditioner the most. This provides ample time to clean, inspect and diagnose your air conditioner before it is turned on. To learn more about getting your home air conditioner maintained, call Garner Heating & Air Conditioning today.
If you'd like to know what your neighbors in Niederwald, TX think, just check out their reviews below!
Recent Jobs and Reviews in Niederwald, TX
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Job Locations and Reviews
Performed heater tune-up. Checked electrical, mechanical, safety, and performance of the system. I cleared the drain line and flow tested the drain with two gallons of water. I also treated the drain line. The filter for the furnace was replaced. No major issues were found, and the system is running at the completion of service.
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Completed duct sealing. Sealed all buckets and returns to the drywall from the attic, with the exception of the laundry room, which was already sealed from the inside. Removed satellite plenum and installed sheet metal wyes to increase airflow. Ran new 8” flex duct. Removed wye going to bedrooms and made them into home runs to the supply plenum. Upsized bucket and sealed to the drywall. Verified drain operation.
Air Conditioning System Repairs: While troubleshooting a client’s AC unit, I found a clogged drain line causing water to back up into the system, threatening internal components. I cleared the clog and installed a float switch to prevent future overflows, ensuring the system would function smoothly throughout the autumn season.
Service diagnostic found that the condensate drain line was clogged. Water had backed up into the secondary drain line and tripped the safety switch. Options for repair were presented to the customer, and Mary chose to have the drain line cleared today. I cleared the drain line and tested the drain with two gallons of water. Clear water was observed flowing from the drain line outside the home. I then treated the drain. I function tested the system and the system is now operational.
Heating tune-up completed on a horizontal gas system. I did find that the inducer motor is slightly over amping and brought this to the attention of the homeowner. He is aware and will help us monitor. No other major issues found, and the system is heating properly at this time.
Performed diagnostic on the system and found that the blower motor has failed. I confirmed the motor is receiving a constant 24volts and 120volts from the furnace board. I presented my findings to the homeowner, and he chose to have the motor replaced and also have a surge protector installed on the furnace. I installed the motor and the surge protector at the furnace. I then cycled power at the thermostat. The total furnace static reading is .56 and the airflow is set to 1085 CFM on the 3-ton system. After checking the airflow, I wiped down the furnace as best as I could.
On arrival, the customer stated that the unit stopped working overnight. I began by checking the air filter, and then replaced it with a customer supplied filter. I then examined the evaporator coil and checked the float switch. I found that the float switch has tripped. Went outside to examine the condenser and found a faulty capacitor. Presented the customer with options for repair, and they chose to move forward with the items on the critical repair estimate. After replacing the capacitor, I vacuumed out, flushed and cleared the condensation drain line with CO2. Poured multiple gallons of water and was able to verify proper drainage before treating the drain line with Viper treatment. Cycled the system on cool mode to verify proper operation of unit. The system is cooling at this time.
Performed cooling maintenance on one heat pump system. Checked all electrical mechanical and performance of the system. Cleared and treated the drain line and washed the outdoor coil. I found the system does not have a water safety switch and there is some microbial growth at the air handler. I cleaned the microbial growth as best as I could. At the condenser I secured the compressor wiring to prevent any rub outs. The condenser fan motor is also showing signs of overheating. No other major issues found.
Duct Air Purifier Installation: Installed duct air purifiers to reduce pollutants and improve indoor air quality with advanced purification technology.
Single system cooling maintenance completed on a horizontal gas system. Indoor unit, fan and evaporator coil are clean. The drain line flushed and treated. The float switch was tested and is operational. Also replaced 4" media filter. The outdoor coils are clean, all electrical within manufacture specs and the refrigerant charge is within range. No major issues found.
Cool check completed on an up-flow air handler and condenser. The drain line has been cleared and treated. The float switch was checked and is working properly. The evaporator coil has significant buildup and I highly recommended it be cleaned in place. The condenser coils have been cleaned. All electrical is within manufactures specs. No other major issues found, and the system is cooling to the best of its ability at time of departure.
Performed AC cool check. Checked electrical, mechanical, safety, and performance of the system. The drain line was cleared and treated. The filter was replaced with a customer supplied filter. The blower wheel is clean. The wiring is tight and in good condition. The secondary drain line is piped in a way that would allow water to back flow into the secondary pan. The condenser fan motor and contactor are both in good condition. The condenser capacitor is within value. The refrigerant charge is within spec, and the condenser coil was cleaned. Options to upgrade the drain line and install a second safety switch were presented to the customer, and homeowner chose to have the safety switch installed. I added a safety switch to the secondary drain line so that water will trip the switch before it flows into the secondary pan. The system was function checked and is running at the time of departure.
AC Refrigerant Leak Repair: Fixed a refrigerant leak and recharged the AC system to restore its cooling capacity and efficiency.
AC Expansion Valve Adjustment: Adjusted a faulty expansion valve to optimize the AC system's cooling performance.
Cool check completed on a horizontal gas system. Cleared and treated the drain line. Checked the float switch and it is operational. The blower wheel is clean. Condenser coils are clean, and the refrigerant levels are within range. I did find that the capacitor is starting to fail. Presented my findings to the homeowner and they decided to have the capacitor replaced today. Completed repair and cycled the thermostat. The system is operational upon departure.
Upon arrival, the customer stated that the outdoor unit was making a humming sound. I verified the blower motor was running. Proceeded outside to inspect the heat pump and discovered that the capacitor has failed. Presented the customer with options to replace the capacitor, and they have decided to move forward with the repair. Replaced the capacitor, and verified the unit was cooling.
Cool check completed on a horizontal gas system. Replaced 4" media filter. The drain line was cleared and treated. Condenser coils clean. No major issues were found, and the system is operating properly at this time.
Performed AC cool check. Checked electrical, mechanical, safety, and performance of the system. The air handler and blower wheel are clean. The drain line was cleared and treated. The wiring is tight and in good condition. The condenser fan motor and contactor are in good condition. The capacitor for the condenser is within value. The refrigerant charge is within factory specifications. The condenser coil was cleaned. No major issues were found, and the system is running at the time of departure.
On arrival the customer stated that the outdoor unit would not turn on. I performed a diagnostic on the system and found that the outdoor capacitor had failed. I informed the homeowner, and he chose to have the capacitor replaced at this time. After I replaced the capacitor, I cycled power at the thermostat and the system is now operational.
Installed ductless system. Mounted wall bracket and installed line hide. The electricians ran high voltage and installed a disconnect. Pressure tested and pulled a vacuum on the copper line set. Verified system operation.
On arrival the customer informed me that his thermostat is on and the system is working but he is unable to change the temperature setting or mode setting on the thermostat. I checked all the wiring and confirmed everything is nice and tight. I then confirmed the thermostat is receiving the proper 24 volts. I offered a replacement T6 thermostat to the customer and he chose to have it replaced at this time. I installed the new thermostat and cycled power. No other major issues were found, and the system is operational at this time.
Performed AC cool check. Checked electrical, mechanical, safety, and performance of the system. The drain line was cleared and treated. The blower wheel is clean. The filter was replaced with a homeowner supplied filter. Low voltage wiring was tightened on the furnace control board terminal block. The condenser coil is clean. The condenser fan motor and contactor are in good condition. The capacitor is within value and the refrigerant charge is within factory specifications. The electrical panel on the condenser unit was treated with JS insecticide to combat ants. No major issues were found, and the system is running at the time of departure.
Performed AC cool check. Checked electrical, mechanical, safety, and performance of the system. The drain line was piped in a way that prevented effective clearing. I did clear the drain as well as I could, and flow tested it with water. I also treated the drain. There is no safety float switch installed. The blower wheel is clean. Low voltage control wiring was tightened. The insulation around the suction line at the evaporator coil was loose and causing the line to sweat so I taped the insulation back together. The condenser fan motor and contactor are in good condition. The condenser capacitor is within value and the refrigerant is within factory specifications. Condenser electrical panel was treated with JS insecticide to keep ants away from the electrical wiring. I also cleaned the condenser coil. No other major issues found.
Performed service diagnostic. Diagnostic found that the condensate drain line was clogged. Water was running out of the secondary drain line. The drain line was not draining well due to lack of slope and there was no way to effectively clear or treat the drain line. Options for repair were presented to the customer and she chose to have the drain re-piped today. I cut out the old section of drain line and cleared the drain. I rebuilt the section with a trap and vents to allow for good water flow and for clearing the drain. I also insulated the drain line. I then flow tested the drain with water and treated the drain. System was running at the time of departure.
On arrival, the customer informed me that her air handler was leaking water. I performed a diagnostic on the system and found that the primary drain line by the condenser was blocked by mud which was preventing the water from draining out. This caused water to back up into the primary drain pan and spill out. I cleared and treated the drain line and tested it with a gallon of water. No other major issues were found and the system is operational at this time.
It was a pleasure serving you and your family. We really appreciate you taking the time to share your feedback with us and the community.